Posts: 12
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Joined: Jan 2018
Serviced the trans, changed filters, changed out filter "cap" which was broke and leaking like a siv.
Made new lines and setup a new trans cooler, put it all back together.
Now this thing will go into Reverse, but no Drive...
It gives me the three codes
2511
5517
5587
The 55 codes refer to clutch pack 3 engagement...
Best part is, coach is backed 20' out of the shop and it's starting to sprinkle!
Any help would be appreciated gents.
Obviously I've checked all the plugs, loose wires, trans fluid level, etc
1996 45' Coach 409 Formally owned by a rock star.
60 Series DDEC III, tuned, No Limit Manifold, S475 turbo and Fluidampr
Purchased wrecked, currently redoing all interior and RF wreck damage.
Posts: 4,188
Threads: 635
Joined: Jul 2012
Check your electrical connections. All of those can be tied to bad connections either at sensors or at the Transmission ECU. The 2511 is no speed reading from the rear output shaft sensor. 5517 deals with the shift solenoid and 5587 indicates that the C3 pressure switch did not close at the end of the shift from Neutral to Reverse.
That is the result of Google assistance, not personal knowledge.
Michael Day
1992 Newell 43.5' #281
NewellOwner.com
Posts: 1,532
Threads: 155
Joined: Jul 2012
Shot in the dark....
High speed idle switch engaged? That will keep my coach from going in gear.
Bill Johnson
Birmingham, Alabama
Posts: 12
Threads: 2
Joined: Jan 2018
Yeah, definitely checked all of that already.
1996 45' Coach 409 Formally owned by a rock star.
60 Series DDEC III, tuned, No Limit Manifold, S475 turbo and Fluidampr
Purchased wrecked, currently redoing all interior and RF wreck damage.
Posts: 1,168
Threads: 28
Joined: Mar 2013
Is it possible you are low on trans fluid? We had our oil changed once where the tech drained our transmission by mistake and tried to cover his error by stating that we had a "leak". We had to put 10 qts in to get it out of the bay. Another 6-8 qts on down the road to get it back to proper full level.
(This post was last modified: 01-06-2019, 08:21 AM by
ccjohnson.)
Posts: 208
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Joined: Mar 2013
Take off green wire under dash on parking brake
Ashley Pardue Coach 589
Posts: 5,417
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Joined: Jul 2012
I would really rethink trans fluid level. One, cause you drained some out to change the filters.
Two, cause a pressure switch isnt making, no fluid equal no pressure. Three cause the only way you can test the fluid level right now is with the dipstick instead of using the Allison keypad. You can’t check it with the keypad till its hot, and it will never get hot idling.
It went into reverse sort of negating the high idle and park brake scenarios.
Richard and Rhonda Entrekin
99 Newell, 512
Maverick Hybrid Toad
Inverness, FL (when we're home
)
Posts: 12
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Joined: Jan 2018
Been busy working. Messed with it more this weekend, still doesn't want to go into a forward gear, reverse works fine, fluid level is good on dip stick...
Any Allison "experts" that may have something different? This electronic turd has to say something more...
And my first time re-filling it, I did fill it up more, still didn't do anything.
1996 45' Coach 409 Formally owned by a rock star.
60 Series DDEC III, tuned, No Limit Manifold, S475 turbo and Fluidampr
Purchased wrecked, currently redoing all interior and RF wreck damage.
Posts: 487
Threads: 14
Joined: Nov 2012
I'm with Richard on "no pressure". I am not an Allison wizard. I asked one of my shop guys to check the level and later discovered they did not check it with the engine running. It's high when the engine is off so if you have a normal level with no engine running, this might be the answer.
Gordon Jones
2000-45'-2slide-#567
Posts: 30
Threads: 0
Joined: Oct 2012
Is it a push button or toggle shifter? If its a toggle it could be the Stone Bennett shifter not shifting working correctly. Are the codes historical or active. If active codes then I would lean towards internal issues.