You are not logged in or registered. Please login or register to use the full functionality of this board...


Cooling Fan - Multi-Wing Z Series Fan
#11

New blades installed pitched to 27.5°.

   
   
   
   
   
   

Kristi & Jeff King
Bentonville, Arkansas
#744 2005 45’ Newell Coach 
ZF Suspension/Active Steering Tag Axle
CAT-13 ACERT KCB Engine 525HP 1642 ftlbs Torque Cat Compound Turbocharger 43.5 psi
Allison HD4000MH Transmission with PTO drive.
Reply
#12

Looking forward to seeing how it performs. Nice work!

--Simon
1993 8v92TA #312
Reply
#13

Beautiful workmanship, very clean. To bad you could rig it up like a constant speed prop.

1999 45'  #504 "Magnolia"
Gravette, Arkansas
1996 40 XL Prevost Marathon 
Reply
#14

(05-01-2023, 07:29 AM)jdkskyking Wrote:  Again, Richard encouraged me to take a deep dive and tackle a complicated project. Thank you Richard!

I removed my Multi-Wing Fan to re-pitch the blade angle. It’s also the perfect opportunity to clean the radiator/CAC/hydraulic cooler!

Read the Multi-Wing Fan instructions thoroughly!




My fan has eight Z6 blades that were set at 20° pitch. I am going to increase the blade angle to 32.5° in an effort to draw more air across the radiator stack. I hope this also helps move hot air out the back of the engine bay as well.

My Multi-Wing Fan was manufactured 5/26/04. 

I measured the diameter of the fan at 38”.

The blades are in good condition, I may consider replacing them in the future due to age. 

Tools used in removal:
The center bolt which holds the fan assembly to the shaft on the overhung load assembly requires a 1/2” wrench, the bolt has a thread of 5/16-24. I forgot to measure the bolt length.
 
The remaining hardware was removed with a 10mm wrench and socket. 




Removal:
The entire Multi-Wing Fan can be removed from the drive assembly by removing the center bolt that threads into the OHLA drive shaft (I noticed a coach with a C-15 did not have a OHLA but the motor appeared to be similar to my motor). 
I opted to leave the fan mounting flange attached to shaft by removing the five M6-1.0 bolts and lock nuts. I used a 1/8” ball rotary file in a Dremel tool to make a small mark on the flange and hub to ensure I re-assemble in the original configuration. Yes this created more work for me but I’m not familiar with a tapered key shaft assembly. As I mentioned, I did remove the bolt for a photo shoot opportunity then replaced it. 


Clearly, the left side of the engine compartment is tight quarters and removing the fan assembly is not a desirable job. I strongly suggest a long sleeve shirt for this job because it is necessary to reach your arm through the fan blades. They do have sharp edges. 
Patients is needed when loosening the bolts/nuts to remove the fan from the flange. I have an electric Milwaukee 3/8” ratchet that was very helpful. 

Once the fan assembly was free of the flange, I had to strap a coolant header tank hose out of the way and remove the CAC boot so the fan could slide out of the engine bay.


Once I had the assembly in the workshop and on a flat surface, it was photo shoot time. 
I took several pictures OF EVERYTHING to aid in re-assembly. On my fan two of the outer bolts had additional lock nuts (one a cap nut) added for balancing. 
I purchased new bolts and nuts and reassemble in the original configuration. 

The next step is identifying/marking all of the blades and hub/retainer configuration. 


The outer ring of bolts are the M6-1.0x25
The inner bolts are M6-1.00x16

TAKE MORE PHOTOS THAN YOU’LL EVER NEED. 

I used plastic pry tools to separate the hub and retaining rings. Do this step slowly because you want to note which “grove” the pitch locating pin is in the hub/retainer.


I determined the pitch of my blades were set at 20°. This is minimum pitch the fan can be set at. I honestly don’t know what to think of this setting. The Multi-Wing rep recommended I increased the pitch. Time will tell. 

I proceeded to clean up all of the parts for re-assembly making sure not to wash off the information I wrote on everything. 

I strongly suggest you study and inspect every component carefully. The manufacturer placed a locating triangle in the casting. It just so happened mine was at the 9 o’clock position when I started marking everything. Use the triangle to make sure the retainer and hub are re-assembled in the original configuration. 

Once I figured out where I needed to place the locating pin in the retainer ring for 32.5°, it was time to start the re-assembly process. 
I used clamps to hold the blades in the correct position as I placed the hub over the retaining ring. I used C-Clamps to hold the hub and retaining ring together. 



I’ll continue the assembly in the next post.

How did you get the fan motor to stay still while taking off the outside screw?  My blades are spinning free and need to be replaced but when I turn the screw on the outside, the motor turns and it doesn't loosen.

Corey and Katherine O'Brien
1998 Newell Coach 469
Reply
#15

It wasn’t easy but I inserted my left arm/hand and wrench between the blades and, wearing a glove on my right hand, held on to the blades.

Another option is to remove the blade assembly by removing the bolts/nuts that hold it on the “hub”.

Kristi & Jeff King
Bentonville, Arkansas
#744 2005 45’ Newell Coach 
ZF Suspension/Active Steering Tag Axle
CAT-13 ACERT KCB Engine 525HP 1642 ftlbs Torque Cat Compound Turbocharger 43.5 psi
Allison HD4000MH Transmission with PTO drive.
Reply
#16

   

Kristi & Jeff King
Bentonville, Arkansas
#744 2005 45’ Newell Coach 
ZF Suspension/Active Steering Tag Axle
CAT-13 ACERT KCB Engine 525HP 1642 ftlbs Torque Cat Compound Turbocharger 43.5 psi
Allison HD4000MH Transmission with PTO drive.
Reply
#17

Yea but on mine the blades are free spinning so when I turn the bolt it turns the motor and not the blades so I have nothing to hold on to to stop the axle from spinning.  Any idea how I can stop the fan motor from spinning as I wrench on the bolt?  I have attached a few pictures.  I can get my hand in there because one of the blades flew off completely so there is plenty of room to get in there.

Here is a small video of how it is free spinning.

Radiator Fan Movement


Attached Files Thumbnail(s)
       

Corey and Katherine O'Brien
1998 Newell Coach 469
Reply
#18

Well, you got a doozy there. The video was extremely helpful. Thanks for posting.

I don’t know if any of this will work. But it is some of the redneck engineering I would try first.

First attempt, wrap 1/8 nylon twine, mason’s cord, or nylon rope around the shaft behind the fan hub. Put five or six wraps on the shaft so that the cord will tighten as you try to loosen the bolt. IIRC correctly the bolt is 1/4 28 right hand. Of. Course tie the cord to the cross member to hold it as you turn the bolt. You may have to apply tension to the loose end to make the cord grip. Imagine how a capstan works.

Second attempt. Buy a 1 1/2 or 2 inch wide piece of 1/8 or 3/16 flatstock at ACE or Lowes/HD. Cut a v notch in the end. The deeper the V, the more grip it will have. Wedge the v onto the shaft.


Third option, by far the most work, but almost guaranteed. Remove the two bolts that hold the hyd motor to the overhung load adaptor. The motor is heavy so be prepared. The motor shaft is splined and will slip out of the OHLA. This will give you access to the back of the OHLA. However the back of the OHLA shaft will be a female spline fit so you will have to wedge something (brass or aluminum to keep from messing up the splines) into the back of the shaft to keep it from turning.

Fourth option. You could remove the in and out lines on the hyd motor and cap them, effectively locking the motor. However, those lines are below the reservoir, so when taken loose, all the ATF in the reservoir is going to drain. BIG MESS.

Fifth option, use an oscillating saw and cut the plastic hub into two or three pieces so you can remove the fan from the shroud.



Maybe this will spur some creative solutions by other gurus.

Richard and Rhonda Entrekin
99 Newell, 512
Maverick Hybrid Toad
Inverness, FL (when we're home Cool )
Reply
#19

You might want to disassemble the entire fan and remove it piece by piece do you can have a better chance at using Richard’s recommendations.

You need a complete new fan assembly.

Kristi & Jeff King
Bentonville, Arkansas
#744 2005 45’ Newell Coach 
ZF Suspension/Active Steering Tag Axle
CAT-13 ACERT KCB Engine 525HP 1642 ftlbs Torque Cat Compound Turbocharger 43.5 psi
Allison HD4000MH Transmission with PTO drive.
Reply
#20

Agreed the hub is beyond repair, so new assembly required.

Be careful not to damage the seal around the shaft on the OHLA, or you have a new very messy problem.

One idea came to me during sleep. If you look at the metal H shaped frame that the OHLA is bolted onto, you will see two bolts at the top, and two bolts at the bottom. Removing those four bolts allows some pivoting and moving of the entire assembly without disconnecting the hydraulic hoses. It may take a helper on the bottom two bolts. One on the nut under the coach, and one to hold the top of the bolt.

DO NOT crawl under the coach without proper support. You never know what can happen, and having 50k pounds sit down on you will totally ruin Katherine’s day.

Where are you? In case there are any of the Hee Haw gang close by.

Richard and Rhonda Entrekin
99 Newell, 512
Maverick Hybrid Toad
Inverness, FL (when we're home Cool )
Reply


Forum Jump:


Users browsing this thread: 8 Guest(s)